Southern Oregon State College Computing Sciences Building
POWER SAVE
P.O. Box 880, Cottage Grove, OR. 97424 1-541-942-5560, FAX
1-541-942-4682
Testing Of LPA Retrofit Technology
Southern Oregon State College
Computing Sciences Building
Ashland, Oregon
80 Ton Trane Chiller
Test Period: June 11-20, 1996
Report Date: August 7, 1996
Prepared by: Gene Madison M.E., Power Save
TABLE OF CONTENTS
OVERALL TEST RESULTS SUMMARY
Test System
Theory of LPA Retrofit Technology
Testing Objectives
Testing Equipment
Testing Period
OVERALL TEST RESULTS
General Background of Test
Overall Savings and Savings Factor
PROCESS TEST RESULTS BY TEMPERATURE CELL
Operating Parameters
NATIONAL ENVIRONMENTAL IMPACT
PROJECT LOCATION PHOTOGRAPHS
TEST REPORT AND ANALYSIS
Chiller Data With and Without LPA Operational
TABLES and GRAPHS
Head Pressure vs Ambient Temperature
Table - Averaged Test Results With
LPA Retrofit Technology
DISCUSSION OF DATA GRAPHS
Figure 1. Percentage Savings with Ambient
Temperature
Figure 2. Head Pressure with Ambient Temperature
Figure 3. Compression Ratio with Ambient
Temperature
Figure 4. Liquid Injection Temperature with Ambient
Temperature
Figure 5. Liquid Line Temperature with Ambient
Temperature
Figure 6. Compressor kW with Ambient Temperature
Figure 7. Compressor Capacity with Ambient
Temperature
Figure 8. Compressor kW/Ton with Ambient
Temperature
APPENDIX
TRANE COMPRESSOR DATA
Manufacturer's Performance Data Analysis
Compressor Performance
Savings Per Degree Reduction in SCT vs Reduced
Condensing Temperature
40-Ton Trane Compressor Performance
OVERALL TEST RESULTS SUMMARY
The LPA Retrofit project and testing objectives to verify the conservative project
forecast energy savings rate of 1.4%/F were met. The overall test results at the
test average of 65.8F and over the range of 48F to 78F show an energy savings rate of
1.78% per degree F reduction in the saturated condensing temperature (SCT) of R-22.
This compares very favorably (16% higher) with Trane's Performance data of 1.53%
per degree F at the ambient test average of 65.6F. This increase is due in part to the
increased condenser surface area available at the maximum compressor loading of 50%
experienced during this test. Based on the building load being carried by No. 1 as the
lead chiller, this projects to an annual forecast of 35.3% for an estimated savings
of 116,500 kWh/yr. using Trane's median rate of 1.53%/F (see Appendix for
spreadsheet calculation). This test clearly demonstrates the savings which are achievable
with the LPA Retrofit Technology applied to the 80 Ton Trane chiller.
The test average kWh/hr savings with the LPA Retrofit were 31%; correcting for the
average ambient of 65.8F normalized the savings to 26.3%. The liquid injection circuit
reduced the hot gas temperature by 60F from 165F to 105F. As the condenser capacity
is not limited at or below design conditions (85F-95F), no measured savings from liquid
injection were expected nor measured within the test range of 50F to 75F.
TEST SYSTEM
The system tested was the Trane Air Cooled Chiller Unit No. 1 of 2, a nominal 80 Ton unit
servicing the Computing Sciences Building. This is a Trane Model No. CGAC-C80 Chiller with
two Trane Model No. C40R compressor circuits (both with unloaders). Each circuit was
retrofit with a HY-SAVE LPA860IND Liquid Pressure Amplifier including the installation of
liquid injection into the superheated hot gas line.
It was decided with SOSC management to modify both compressor circuits on a single
chiller rather than the original plan of modifying the lead circuits on both 80 Ton
chillers. This application change was necessitated when it was learned that the Trane
controller could not be adjusted to control a constant lead compressor position.
The subcooler section of each of the Trane condensers was bypassed to reduce overall
pressure drop and subsequently further lower SCT's with the LPA providing the necessary
liquid pressure subcooling for the circuit. The Trane compressor performance data is
included in the Appendix section of this report. Head pressures are maintained by
controlling the air cooled condensing unit fans in the package unit.
THEORY OF LPA RETROFIT TECHNOLOGY
The controls of the OEM Trane chiller units are factory set to maintain a minimum head
pressure of approximately 210-220 psig at design conditions in order to maintain the
refrigerant in its pure liquid form at the expansion valve. This is accomplished by
operating one condenser fan at all times and then operating the other fans as ambient
temperatures increases. Reducing the head pressure to achieve energy savings without
Liquid Pressure Amplification, would create flash gas, which would then reduce the cooling
capacity of the system, defeating the attempt to save kWh. Applying the LPA Retrofit
Technology by:
1. Installing HY-SAVE liquid Pressure Amplifiers into the liquid line
of each circuit.
2. Injecting liquid refrigerant into the hot gas lines ahead of the
condenser inlet.
3. Modifying the fan controls on the air condensing unit.
We expect to see the following results:
1. A reduction in head pressure coincident with a drop in ambient
temperatures by maximizing the flow of ambient air across the condensing coil. This
reduces the compression ratio and the necessary compressor work of the refrigeration
cycle.
2. Increased refrigeration efficiency with colder liquid refrigerant
(density and enthalpy) at the TXV.
3. Reduced kW/Ton (or increased EER) from 1 and 2 above.
4. Increased condenser capacity at ambient temperatures over 85F.
5. Reduced hot gas temperatures entering the condenser increasing
condenser surface area and adding system capacity at high ambient temperatures.
If these results are achieved, we expect to see the following benefits over a longer
period of time:
1. Reduced annual energy consumption, kW/yr.
2. Increased system capacity due to the increased enthalpy content of
colder R-22.
3. Increased system capacity at high ambient conditions with liquid
injection.
4. Increased compressor life due to lower head pressures.
5. Decreased service problems due to lower system head pressures.
TESTING OBJECTIVES
The primary objective of this test was to verify the rate of energy savings assumption of 1.4%
per degree F reduction in condensing temperatures used in the initial project savings
forecast as well as the 1.53%/F based on Trane Performance Data.
The secondary objectives of the test were to compare the operating parameters and
efficiencies of this retrofit Trane unit with and without the HY-SAVE LPA Liquid Pressure
Amplifier operational with both compressors retrofit.
TESTING EQUIPMENT
The test equipment used was the DATREX Multi-Channel Data logger. Because of the duration
of the test, the data was logged every 10 seconds and averaged every 5 minutes. The
following parameters were monitored:
Suction Pressure
Head pressure
True kW for Compressor
Suction Temperature
Liquid Line Temperature
Hot Gas Bypass Temperature
Liquid Injection Temperature
Chilled Water In/Out Temperatures
Ambient Temperature
TESTING PERIOD
To assure that all savings were due to the application of the LPA Technology retrofit, all
routine maintenance procedures and adjustments were performed by SOSC's service contractor
before the testing was started. The data logging was initiated on May 30, 1996. The
initial reslults were lost due to internal battery problem with the Datrex. The test
comparison data was logged from June 11-June 20, 1996.
OVERALL TEST RESULTS
General Background of Test
The ambient temperature ranged from the high 40's to the high 70's and the maximum load on
either compressor was 50%. This provided a relatively wide range with adequate load and
sufficiently low ambient to demonstrate the LPA technology. The average temperatures for
both phases of the test for all minutes logged was 65.8F for the w/o LPA test and 62.5F
for the LPA test. The savings calculations were normalized to the w/o LPA test
average.
It is important to note that the data logging equipment does not start and stop when
the compressors turn on; it averages data for each five minute period even though the
compressors may be off or are running from 0 to 100% of the time. Therefore, the only
Accurate method of comparison to calculate the savings is to use the averages
of all of the data for each phase of the test, not the individual data points, or
temperature cell
Averages. This approach takes into account not only the savings with lower head
pressures but improvements in efficiency and subsequently lower run times.
For system comparison while compressors were running, the data was averaged into 5
Degree F cells (avg. 65F = 62.5 to 67.5). Averages of these temperature cells with all
zero run times removed were the graphed to show the relationship of system operating
parameters with ambient temperatures when the compressors are running.
Overall Savings and Savings Factor
As can be seen from the "Averaged Test Results With LPA
Retrofit Technology" table, with the LPA operational, the average
head pressure (including zero run times) dropped from 172 psig (w/o LPA) to 137 psig with
a corresponding reduction in kWh consumption of 31% at the average temperatures of 62.5F
and 65.7F respectively. Correcting for the differences in ambient reduces this to 26.3%.
This corresponds with an average reduction of the R22 condensing temperature from 91.4 to
76.7F, or 14.7F.
The calculated savings factor is the = 26.3%/14.7F = 1.78%/F and is +16% greater than
the 1.53%/F projected from the Trane Performance Data.
When applied to the annual bin hour distribution, the more conservative Trane data of
1.53/F factor yields an annualized savings of 116,500 KWH or 35.3%.
PROCESS TEST RESULTS BY TEMPERATURE CELL
Operating Parameters
For system comparison while compressors were running, the data was averaged into 5 Degree
F cells (avg. 65F = 62.5 to 67.5). Averages of these temperature cells with all data less
than 50% load removed were then compiled to show the relationship of system operating
parameters with ambient temperatures when the compressors are running at 50% load. The
data between cells was smoothed using the incremental sum averaging technique.
The table titled "Averaged Test Results With LPA Retrofit
Technology" summarizes these test results at the average temperature cells.
Graphs also follow for the following characteristics:
Figure 1. Percentage Savings with Ambient
Temperature
Figure 2. Head Pressure with Ambient Temperature
Figure 3. Compression Ratio with Ambient
Temperature
Figure 4. Liquid Injection Temperature with Ambient
Temperature
Figure 5. Liquid Line Temperature with Ambient
Temperature
Figure 6. Compressor kW with Ambient Temperature
Figure 7. Compressor Capacity with Ambient
Temperature
Figure 8. Compressor kW/Ton with Ambient
Temperature
NATIONAL ENVIRONMENTAL IMPACT
In addition to the substantial energy and cost savings, there is a major national
environmental impact from this project in terms of the annual reduced consumption of
hydrocarbons and subsequent emissions approximated as follows: 1.
Reduction in pounds of CO2 = 179,400
2. Reduction in pounds of coal = 123,400 or
Reduction in pounds of gas/oil = 90,000
These numbers are based on national averages compiled by the Rocky
Mountain Institute, 1990.
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